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Chlorinated Solvents |
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Contaminants: Reactive Media: Construction: Point of Contact: |
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A permeable reactive barrier (PRB) was installed in August 1998 at Operable Unit 1 of the Marzone site in Tifton, GA, to remediate ground water contaminated with pesticides and volatile organic compounds (VOCs). The Marzone facility was used as a pesticide formulation facility from 1950 until the 1980s. Soils in this area consist of a mixture of sand, sandy clay, and clay. A shallow aquifer is located at a depth of 7 ft and a deeper aquifer exists at approximately 25 ft. Hydraulic conductivity is estimated at 2.9-4.6 ft/day. The modified funnel-and-gate system comprises a 400-ft barrier wall that was installed using a vibrating beam technology. A collection trench lined with geotextile and filled with granular drain material was constructed upgradient of and parallel to the barrier wall. Ground water collected in this trench moves by way of a slotted well screen and associated piping into treatment vaults containing approximately 1,800 pounds of activated carbon located between the collection trench and barrier wall. From the treatment vaults, ground water moves slowly (1-2 gal/min) by way of piping through the barrier wall and into a distribution trench of similar construction as the collection trench but running perpendicular to the barrier wall. Cleanup goals for the contaminants of concern are: 0.00003 mg/L for alpha-BHC, 0.0001 mg/L for beta-BHC, 0.00077 mg/L for DDD, 0.00054 mg/L for DDT, 10 mg/L for xylene, 0.7 mg/L for ethylbenzene, 0.0002 mg/L for lindane, and 0.0039 mg/L for methyl parathion. Sampling of the treatment vault effluent is conducted on a monthly basis. Contaminant concentrations in the effluent have been below detection levels.
The funnel-and-gate system was selected for use because if offered less impact to the surrounding community than other treatment technologies, while being partially self-operational. Immediately after construction, flushing of the system was required every 3-4 weeks in order to maintain flow. Improvements were made to the system to allow venting of gas pockets which were forming in the system. The activated carbon vaults were also changed to an upflow configuration. Since these improvements were made, the system has been operating effectively. |
Sponsored by the Technology Innovation Program
Date Last Modified: January 14, 2000